]> git.karo-electronics.de Git - karo-tx-linux.git/commit
arm64: dts: h3ulcb: Fix EthernetAVB PHY timing
authorVladimir Barinov <vladimir.barinov@cogentembedded.com>
Wed, 1 Feb 2017 08:42:02 +0000 (09:42 +0100)
committerSimon Horman <horms+renesas@verge.net.au>
Mon, 6 Mar 2017 08:54:26 +0000 (09:54 +0100)
commit5b9fd1962f605a31842371471e559407c293131f
tree7067a04d08d5b7ae5ca095cb07b081d33dc83bdd
parent0e45da1c6ea6b18616d95c697ecd6234bc504ef6
arm64: dts: h3ulcb: Fix EthernetAVB PHY timing

Set PHY rxc-skew-ps to 1500 and all other values to their default values.

This is intended to to address failures in the case of 1Gbps communication
using the by h3ulcb board with the KSZ9031RNX phy.

Signed-off-by: Vladimir Barinov <vladimir.barinov@cogentembedded.com>
Signed-off-by: Takeshi Kihara <takeshi.kihara.df@renesas.com>
Signed-off-by: Simon Horman <horms+renesas@verge.net.au>
arch/arm64/boot/dts/renesas/r8a7795-h3ulcb.dts