]> git.karo-electronics.de Git - karo-tx-linux.git/commitdiff
arm64: dts: r8a7795: salvator-x: Fix EthernetAVB PHY timing
authorKazuya Mizuguchi <kazuya.mizuguchi.ks@renesas.com>
Wed, 1 Feb 2017 08:42:01 +0000 (09:42 +0100)
committerSimon Horman <horms+renesas@verge.net.au>
Mon, 6 Mar 2017 08:54:26 +0000 (09:54 +0100)
Set PHY rxc-skew-ps to 1500 and all other values to their default values.

This is intended to to address failures in the case of 1Gbps communication
using the by salvator-x board with the KSZ9031RNX phy. This has been
reported to occur with both the r8a7795 (H3) and r8a7796 (M3-W) SoCs.

Signed-off-by: Kazuya Mizuguchi <kazuya.mizuguchi.ks@renesas.com>
Signed-off-by: Takeshi Kihara <takeshi.kihara.df@renesas.com>
Signed-off-by: Simon Horman <horms+renesas@verge.net.au>
arch/arm64/boot/dts/renesas/r8a7795-salvator-x.dts

index dc1177c76aa5eaaa640338beb50a487382c8b6c8..5158ba3f9ce3f6d2f932f6927170343bc52c9b19 100644 (file)
        status = "okay";
 
        phy0: ethernet-phy@0 {
-               rxc-skew-ps = <900>;
-               rxdv-skew-ps = <0>;
-               rxd0-skew-ps = <0>;
-               rxd1-skew-ps = <0>;
-               rxd2-skew-ps = <0>;
-               rxd3-skew-ps = <0>;
-               txc-skew-ps = <900>;
-               txen-skew-ps = <0>;
-               txd0-skew-ps = <0>;
-               txd1-skew-ps = <0>;
-               txd2-skew-ps = <0>;
-               txd3-skew-ps = <0>;
+               rxc-skew-ps = <1500>;
                reg = <0>;
                interrupt-parent = <&gpio2>;
                interrupts = <11 IRQ_TYPE_LEVEL_LOW>;