From: Fabio Estevam Date: Wed, 12 Apr 2017 21:31:18 +0000 (-0300) Subject: ARM: dts: imx53-qsrb: Pulldown PMIC IRQ pin X-Git-Tag: v4.12-rc2~20^2~4^2~2 X-Git-Url: https://git.karo-electronics.de/?a=commitdiff_plain;h=2fe4bff3516924a37e083e3211364abe59db1161;p=karo-tx-linux.git ARM: dts: imx53-qsrb: Pulldown PMIC IRQ pin Currently the following errors are seen: [ 14.015056] mc13xxx 0-0008: Failed to read IRQ status: -6 [ 27.321093] mc13xxx 0-0008: Failed to read IRQ status: -6 [ 27.411681] mc13xxx 0-0008: Failed to read IRQ status: -6 [ 27.456281] mc13xxx 0-0008: Failed to read IRQ status: -6 [ 30.527106] mc13xxx 0-0008: Failed to read IRQ status: -6 [ 36.596900] mc13xxx 0-0008: Failed to read IRQ status: -6 Also when reading the interrupts via 'cat /proc/interrupts' the PMIC GPIO interrupt counter does not stop increasing. The reason for the storm of interrupts is that the PUS field of register IOMUXC_SW_PAD_CTL_PAD_CSI0_DAT5 is currently configured as: 10 : 100k pullup and the PMIC interrupt is being registered as IRQ_TYPE_LEVEL_HIGH type, which is the correct type as per the MC34708 datasheet. Use the default power on value for the IOMUX, which sets PUS field as: 00: 360k pull down This prevents the spurious PMIC interrupts from happening. Commit e1ffceb078c6 ("ARM: imx53: qsrb: fix PMIC interrupt level") correctly described the irq type as IRQ_TYPE_LEVEL_HIGH, but missed to update the IOMUX of the PMIC GPIO as pull down. Fixes: e1ffceb078c6 ("ARM: imx53: qsrb: fix PMIC interrupt level") Signed-off-by: Fabio Estevam Signed-off-by: Shawn Guo --- diff --git a/arch/arm/boot/dts/imx53-qsrb.dts b/arch/arm/boot/dts/imx53-qsrb.dts index de2215832372..4e103a905dc9 100644 --- a/arch/arm/boot/dts/imx53-qsrb.dts +++ b/arch/arm/boot/dts/imx53-qsrb.dts @@ -23,7 +23,7 @@ imx53-qsrb { pinctrl_pmic: pmicgrp { fsl,pins = < - MX53_PAD_CSI0_DAT5__GPIO5_23 0x1e4 /* IRQ */ + MX53_PAD_CSI0_DAT5__GPIO5_23 0x1c4 /* IRQ */ >; }; };