From: Marek Vasut Date: Mon, 1 Apr 2013 23:29:29 +0000 (+0200) Subject: ARM: mxs: Slow down the I2C clock speed X-Git-Url: https://git.karo-electronics.de/?a=commitdiff_plain;h=55985e15b80beb339d3e332f00a26003deff14e6;p=linux-beck.git ARM: mxs: Slow down the I2C clock speed Slow down the I2C clock speed on M28 and SPS1 as it turns out the I2C block in i.MX28 can not operate stable enough with the bus running at 400kHz. Note that the driver used by Freescale runs the bus at 250kHz when 400kHz speed is selected, but the mainline Linux kernel runs the bus at actual 400kHz and that's where it is occasionally unstable. Play safe and run the bus at 100kHz. Signed-off-by: Marek Vasut Cc: Fabio Estevam Signed-off-by: Shawn Guo --- diff --git a/arch/arm/boot/dts/imx28-m28evk.dts b/arch/arm/boot/dts/imx28-m28evk.dts index 6ce3d17c3a29..fd36e1cca104 100644 --- a/arch/arm/boot/dts/imx28-m28evk.dts +++ b/arch/arm/boot/dts/imx28-m28evk.dts @@ -152,7 +152,6 @@ i2c0: i2c@80058000 { pinctrl-names = "default"; pinctrl-0 = <&i2c0_pins_a>; - clock-frequency = <400000>; status = "okay"; sgtl5000: codec@0a { diff --git a/arch/arm/boot/dts/imx28-sps1.dts b/arch/arm/boot/dts/imx28-sps1.dts index e6cde8aa7fff..6c6a5442800a 100644 --- a/arch/arm/boot/dts/imx28-sps1.dts +++ b/arch/arm/boot/dts/imx28-sps1.dts @@ -70,7 +70,6 @@ i2c0: i2c@80058000 { pinctrl-names = "default"; pinctrl-0 = <&i2c0_pins_a>; - clock-frequency = <400000>; status = "okay"; rtc: rtc@51 {